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Using the Turnigy Talon Frame I have built this sturdy little 330 ACRO Quadcopter. Running a Turnigy 2200mA 4s Nanotech Lipo. This video is is running KK2.1 FW 1.6 and it loses Self Level after some sharp turning. Not great. I upgraded to Steveis SW 1.12S1 beginner and it has resolved this problem and flys as it should. I will post a video of this configuration soon.
Talon Turnigy V2 frame cut to 333 in size
Turnigy 2830/11 1000kV Motors
AFRO 30A ESCs SimonK
9 x 4.7 Props
KK2.1 Controller
X330 Base Plate for battery mount.
Flying time 8-9 mins
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